Thursday, 29 April 2010
Suraj Conclusion
I feel that the project was fairly successful, even though the robot didnt work correctly on the demonstration day. We made great progress and had the robot following the line. We have included a video of the robot following the line and then turning to the left. We then attempted to improve the robot so that it will also turn to the right, and then stop once it reached a solid line from left to right. In the process of doing this we hit a dead end. A problem occurred which made the robot completely useless. We believe that the microchip used had been damage in some way. We realised this after we had improved the coding and then attempted to reprogram the chip. However there is some light at the end of the tunnel. it was a great learing curve and i feel that if we had a replacement mirco chip we would have been able to reprogram it and have the robot working.
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